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-rw-r--r--drivers/power/Kconfig9
-rw-r--r--drivers/power/axp209.c23
2 files changed, 32 insertions, 0 deletions
diff --git a/drivers/power/Kconfig b/drivers/power/Kconfig
index e83036fd66..9495dca33b 100644
--- a/drivers/power/Kconfig
+++ b/drivers/power/Kconfig
@@ -231,6 +231,15 @@ config AXP_ALDO3_VOLT_SLOPE_08
endchoice
+config AXP_ALDO3_INRUSH_QUIRK
+ bool "axp pmic (a)ldo3 inrush quirk"
+ depends on AXP209_POWER
+ default n
+ ---help---
+ The reference design denotes a value of 4.7 uF for the output capacitor
+ of LDO3. Some boards have too high capacitance causing an inrush current
+ and resulting an AXP209 shutdown.
+
config AXP_ALDO4_VOLT
int "axp pmic (a)ldo4 voltage"
depends on AXP209_POWER
diff --git a/drivers/power/axp209.c b/drivers/power/axp209.c
index cf138fc722..67b420910c 100644
--- a/drivers/power/axp209.c
+++ b/drivers/power/axp209.c
@@ -122,6 +122,29 @@ int axp_set_aldo3(unsigned int mvolt)
if (rc)
return rc;
+#ifdef CONFIG_AXP_ALDO3_INRUSH_QUIRK
+ /*
+ * On some boards, LDO3 has a too big capacitor installed. When
+ * turning on LDO3, this causes the AXP209 to shutdown on
+ * voltages over 1.9 volt. As a workaround, we enable LDO3
+ * first with the lowest possible voltage. If this still causes
+ * high inrush currents, the voltage slope should be increased.
+ */
+ rc = pmic_bus_read(AXP209_OUTPUT_CTRL, &cfg);
+ if (rc)
+ return rc;
+
+ if (!(cfg & AXP209_OUTPUT_CTRL_LDO3)) {
+ rc = pmic_bus_write(AXP209_LDO3_VOLTAGE, 0x0); /* 0.7 Volt */
+ mdelay(1);
+ rc |= pmic_bus_setbits(AXP209_OUTPUT_CTRL,
+ AXP209_OUTPUT_CTRL_LDO3);
+
+ if (rc)
+ return rc;
+ }
+#endif
+
if (mvolt == -1) {
cfg = AXP209_LDO3_VOLTAGE_FROM_LDO3IN;
} else {