Age | Commit message (Collapse) | Author |
|
correction in delay implementation before we exit out of tx timeout.
Signed-off-by: Chaitanya Sakinam <chaitanya.sakinam@nxp.com>
Reviewed-by: Priyanka Jain <priyanka.jain@nxp.com>
|
|
Add support for AQR113C PHY
Signed-off-by: Madalin Bucur <madalin.bucur@oss.nxp.com>
Reviewed-by: Priyanka Jain <priyanka.jain@nxp.com>
|
|
The next DPMAC was always verified if it is enabled. In case of
DPMAC@6, the DPMAC@7 is verified. As DPMAC@7 is disabled, DPMAC@6 will
be considered disabled and not detected by uboot.
Signed-off-by: Grigore Popescu <grigore.popescu@nxp.com>
Signed-off-by: Ioana Ciornei <ioana.ciornei@nxp.com>
Reviewed-by: Priyanka Jain <priyanka.jain@nxp.com>
|
|
The fdt_fixup_pcie_ls() scans all PCI devices and assumes that all PCI
root devices are layerscape PCIe controllers. Unfortunately, this is not
true for the LS1028A. There is one additional static PCI root complex
(this contains the networking devices) which has nothing to do with the
layerscape PCIe controllers. On recent U-Boot versions this results in
the following panic:
"Synchronous Abort" handler, esr 0x96000044
elr: 000000009602fa04 lr : 000000009602f9f4 (reloc)
elr: 00000000fbd73a04 lr : 00000000fbd739f4
x0 : 0080000002000101 x1 : 0000000000000000
x2 : 00000000fbde9000 x3 : 0000000000000001
x4 : 0000000000000000 x5 : 0000000000000030
x6 : 00000000fbdbd460 x7 : 00000000fbb3d3a0
x8 : 0000000000000002 x9 : 000000000000000c
x10: 00000000ffffffe8 x11: 0000000000000006
x12: 000000000001869f x13: 0000000000000a2c
x14: 00000000fbb3d2cc x15: 00000000ffffffff
x16: 0000000000010000 x17: 0000000000000000
x18: 00000000fbb3fda0 x19: 0000000000000800
x20: 0000000000000000 x21: 00000001f0000000
x22: 0000000000000800 x23: 0000000000000009
x24: 00000000fbdc3c1b x25: 00000000fbdc28e5
x26: 00000000fbdcc008 x27: 00000000fbdc16e2
x28: 000000000f000000 x29: 00000000fbb3d3a0
Code: 394072a1 f94006a0 34000041 5ac00a94 (b8336814)
Resetting CPU ...
This bug already existed in former versions, but the spurious write was
never trapped, because the destination address was a valid address (by
pure luck).
Make sure the PCI root is actually one of the expected PCIe layerscape
controllers by matching its compatible string.
Signed-off-by: Michael Walle <michael@walle.cc>
Reviewed-by: Vladimir Oltean <vladimir.oltean@nxp.com>
Tested-by: Heiko Thiery <heiko.thiery@gmail.com>
Reviewed-by: Priyanka Jain <priyanka.jain@nxp.com>
|
|
The GPIO pins used by the SDHCI controller need to be configured to
allow the interface to work.
Signed-off-by: John Robertson <john.robertson@simiatec.com>
|
|
The existing driver is not compatible with the Driver Model.
This patch makes the necessary changes while also removing obsolescent
calls/properties as follows:
- fdtdec_* calls replaced with dev_read_* equivalents;
- 'clock-freq-min-max' property replaced by querying the frequency of
the source clock 'base_clk';
- The card detect erratum workaround is applied during probe rather than
overriding get_cd.
The card detect workaround (Microchip ref. DS80000736E, erratum #15) is
not always needed and can be disabled using a vendor specific DT
property.
Signed-off-by: John Robertson <john.robertson@simiatec.com>
|
|
Fix build failure, it used to get this implicitly through common.h
until f7ae49fc4f (common: Drop log.h from common header).
Signed-off-by: Rasmus Villemoes <rasmus.villemoes@prevas.dk>
Reviewed-by: Heiko Schocher <hs@denx.de>
|
|
Somewhere between v2020.04 and v2020.07 the mpc8xxx_spi driver broke,
I'm guessing due to this hunk
@@ -559,6 +560,8 @@ int dm_gpio_set_dir_flags(struct gpio_desc *desc, ulong flags)
if (ret)
return ret;
+ /* combine the requested flags (for IN/OUT) and the descriptor flags */
+ flags |= desc->flags;
ret = _dm_gpio_set_dir_flags(desc, flags);
from commit 695e5fd5469a ("gpio: update dir_flags management"). But
the blame is mostly on the driver itself which seems rather confused:
The chip select gpios are requested with GPIOD_ACTIVE_LOW, but then in
each activate/deactivate, dm_gpio_set_dir_flags() is called with
merely GPIOD_IS_OUT, and then the driver call set_value(0) for
activate.
That used to work, but with the above hunk, the ACTIVE_LOW setting
from the request becomes persistent, so the gpio driver ends up being
asked to set the value to 1 in mpc8xxx_spi_cs_activate().
So drop the dm_gpio_set_dir_flags() calls in the activate/deactivate
functions, and use a value of 1 to mean "logically enabled".
Ideally, I think we should also drop the GPIOD_ACTIVE_LOW from the
request and make it up to the list of gpio cs in DT to indicate
whether that CS is enabled when driven low (as is of course usually
the case), but that requires changing
arch/powerpc/dts/gdsys/gazerbeam-base.dtsi among others, and I don't
have that hardware to test on. I have, however, tested our
own (mpc8309-based) hardware with this change, and I have also tested
that removing the GPIOD_ACTIVE_LOW from the request and updating our
DT as
- gpios = <&spisel 0 0>;
+ gpios = <&spisel 0 GPIO_ACTIVE_LOW>;
still works.
Signed-off-by: Rasmus Villemoes <rasmus.villemoes@prevas.dk>
|
|
https://gitlab.denx.de/u-boot/custodians/u-boot-efi
Pull request for UEFI sub-system for efi-2020-10-rc5 (2)
The following bugs are fixed:
* incorrect online help for setenv and env
* description of function efi_mem_carve_out()
* replace printf() by log_err() in stm32mp1_rng driver
A unit test is provided to check that the boot hart id is provided in the
RISC-V device-tree.
|
|
The logging system provides flexible filtering and enhanced output.
Signed-off-by: Heinrich Schuchardt <xypron.glpk@gmx.de>
Reviewed-by: Sughosh Ganu <sughosh.ganu@linaro.org>
|
|
Currently, after config the clock rate, delay 10ms, this is quite a rough
method. Check the clock stable status in the present status register is
enough.
Tested-by: Ji Luo <ji.luo@nxp.com>
Signed-off-by: Haibo Chen <haibo.chen@nxp.com>
|
|
Use mmc_of_parse() to set the common host properties. That includes
"bus-width", so parsing it can be removed from the driver.
But more importantly, "non-removable" is now respected, which fixes
the usage of eMMC.
Signed-off-by: Andre Heider <a.heider@gmail.com>
Reviewed-by: Konstantin Porotchkin <kostap@marvell.com>
Tested-by: Marek Behún <marek.behun@nic.cz>
|
|
Since the introduction of 'get_cd' callback in sdhci core,
dragonboard410c's MMC interface is broken. It turns out that 'get_cd'
callback checks for the host_caps for validating the chip select. And
since the msm_sdhci driver is not parsing the host_caps from DT, not
all of the cababilities are parsed properly. This results in the MMC
interfaces to be broken.
Hence, fix this by adding a call to 'mmc_of_parse' during driver probe.
Signed-off-by: Manivannan Sadhasivam <manivannan.sadhasivam@linaro.org>
Tested-by: Aníbal Limón <anibal.limon@linaro.org>
Reviewed-By: Ramon Fried <rfried.dev@gmail.com>
Reviewed-by: Jaehoon Chung <jh80.chung@samsung.com>
|
|
Nand writes should skip the bad blocks with "nand write" command.
In case of bad blocks with above 32-bit address, nand_block_isbad()
returns false due to truncated bad block address.
In below code segment,
if (nand_block_isbad(mtd, offset & ~(mtd->erasesize - 1)))
offset is 64-bit and mtd->erasesize is 32-bit, hence the truncation is
happening. Cast 'mtd->erasesize' with loff_t to fix this issue.
Signed-off-by: T Karthik Reddy <t.karthik.reddy@xilinx.com>
Signed-off-by: Michal Simek <michal.simek@xilinx.com>
|
|
On the mt7623 platform, if one port enable fail and other port
enable succeed. It will hang on when using pci enum
because the resource was not released correctly.
Signed-off-by: Chuanjia Liu <Chuanjia.Liu@mediatek.com>
Tested-by: Frank Wunderlich <frank-w@public-files.de>
|
|
The commit 57805f2270c4 ("net: bcmgenet: Don't set ID_MODE_DIS when
not using RGMII") needed to be extended for the case of using the
rgmii-rxid. The latest version of the Rasbperry Pi4 dtb files for the
5.4 now specify the rgmii-rxid.
Signed-off-by: Jason Wessel <jason.wessel@windriver.com>
Tested-by: Petr Tesarik <ptesarik@suse.com>
Signed-off-by: Matthias Brugger <mbrugger@suse.com>
|
|
This commit fixes a serious issue occurring when several network
commands are run on a raspberry pi 4 board: for instance a "dhcp"
command and then one or several "tftp" commands. In this case,
packet recv callbacks were called several times on the same packets,
and send function was failing most of the time.
note: if the boot procedure is made of a single network
command, the issue is not visible.
The issue is related to management of the packet ring buffers
(producer / consumer) and DMA.
Each time a packet is received, the ethernet device stores it
in the buffer and increments an index called RDMA_PROD_INDEX.
Each time the driver outputs a received packet, it increments
another index called RDMA_CONS_INDEX.
Between each pair of network commands, as part of the driver
'start' function, previous code tried to reset both RDMA_CONS_INDEX
and RDMA_PROD_INDEX to 0. But RDMA_PROD_INDEX cannot be written from
driver side, thus its value was actually not updated, and only
RDMA_CONS_INDEX was reset to 0. This was resulting in a major
synchronization issue between the driver and the device. Most
visible behavior was that the driver seemed to receive again the
packets from the previous commands (e.g. DHCP response packets
"received" again when performing the first TFTP command).
This fix consists in setting RDMA_CONS_INDEX to the same
value as RDMA_PROD_INDEX, when resetting the driver.
The same kind of fix was needed on the TX side, and a few variables
had to be reset accordingly (c_index, tx_index, rx_index).
The rx_index and tx_index have only 256 entries so the bottom 8 bits
must be masked off.
Originated-by: Etienne Dublé <etienne.duble@imag.fr>
Signed-off-by: Jason Wessel <jason.wessel@windriver.com>
Tested-by: Petr Tesarik <ptesarik@suse.com>
Signed-off-by: Matthias Brugger <mbrugger@suse.com>
|
|
- This patch moves sata phy powerup from dedicate phy to compphy
and adds invert option for sata powerup routine.
Change-Id: I1b4e8753e2b2c14c6efa97bca2ffc7d2553d8a90
Signed-off-by: zachary <zhangzg@marvell.com>
Signed-off-by: Ken Ma <make@marvell.com>
Reviewed-on: http://vgitil04.il.marvell.com:8080/53601
Reviewed-by: Igal Liberman <igall@marvell.com>
Tested-by: Igal Liberman <igall@marvell.com>
[a.heider: adapt to mainline]
Signed-off-by: Andre Heider <a.heider@gmail.com>
Tested-by: Pali Rohár <pali@kernel.org>
Reviewed-by: Stefan Roese <sr@denx.de>
|
|
- Mostly DFU fixes and r8152 fixes
|
|
- SH serial bugfix
|
|
The size returned by 'getvar partition-size' should be in bytes, not in
blocks as fastboot uses that value to generate empty partition when
running format [1].
Note that the function was already returning the proper size in bytes
for NAND devices (see struct part_info details).
[1]
https://android.googlesource.com/platform/system/core/+/refs/heads/android10-release/fastboot/fastboot.cpp#1500
Signed-off-by: Gary Bisson <gary.bisson@boundarydevices.com>
|
|
It was revealed that when the fastboot_tx_write_str function is called
without the previously initialized fastboot_func->in_req->complete field,
a copy of in_req will be sent to the I/O requests queue without
an initialized field.
Moving a piece of code with the initializing of the
fastboot_func->in_req->complete field above transmit_tx allows to solve
this problem.
Fixes: 65c96757fe9 "usb: fastboot: Convert USB f_fastboot to shared fastboot"
Signed-off-by: yurii.pidhornyi <yurii.pidhornyi@globallogic.com>
|
|
Since the USB HID limits the maximum bandwidth(3072) for interrupt
endpoint transfers, when the bInterval set to 1, we can only support 3
boards to run sdp at the same time. In order to support more boards,
change the bInterval of interrupt endpoint to 3, which will not affect
the transmission speed.
Reviewed-by: Ye Li <ye.li@nxp.com>
Signed-off-by: Sherry Sun <sherry.sun@nxp.com>
Signed-off-by: Peng Fan <peng.fan@nxp.com>
|
|
EP0 has been used to transfer file data in sdp before, but the max
packetsize of ep0 is 64 bytes. So in order to improve the file transfer
speed, here add the EP1_OUT interrupt endpoint which max packetsize is
set to 1024 byte.
After testing, it turns out that using ep1out is twice as fast as using
ep0 while receiving data in sdp.
Signed-off-by: Sherry Sun <sherry.sun@nxp.com>
Reviewed-by: Ye Li <ye.li@nxp.com>
Signed-off-by: Peng Fan <peng.fan@nxp.com>
|
|
Add support to f_sdp to search and load iMX8 container image or iMX8M
FIT image by new UUU command SDPV.
When using the SDPV, the uuu will continue to send out data after first
level boot loader used by ROM. This means uuu won't skip to the offset
of the second boot loader, and the padding data before second boot loader
will be sent out. So we have to search the FIT header or container header
in the buffer that SDP received.
Also change to more common method to exit f_sdp handler not depending on
SPL_FIT_FOUND flag because container loader won't set this.
Signed-off-by: Peng Fan <peng.fan@nxp.com>
|
|
Because the buffer length of sdp usb request is 65, we have to allocate
65 bytes not 64 bytes. Otherwise there is potential buffer overflow.
Signed-off-by: Ye Li <ye.li@nxp.com>
Signed-off-by: Peng Fan <peng.fan@nxp.com>
Reviewed-by: Lukasz Majewski <lukma@denx.de>
|
|
Add HS endpoint descriptor for SDP. So that we can use high speed endpoint,
and the SDP device can send packet with 512 byte size.
Signed-off-by: Ye Li <ye.li@nxp.com>
Signed-off-by: Peng Fan <peng.fan@nxp.com>
Reviewed-by: Lukasz Majewski <lukma@denx.de>
|
|
MAX3420 implements FullSpeed USB Device over SPI.
Another version MAX3421, also implements USB Host mode.
This driver should be good for the device mode of max3421 as well.
Signed-off-by: Jassi Brar <jaswinder.singh@linaro.org>
|
|
Default implementation of fastboot_set_reboot_flag function that depends
on "bcb" commands could be used in general case if there are no need to
make any platform-specific implementation, otherwise it could be
disabled via Kconfig option FASTBOOT_USE_BCB_SET_REBOOT_FLAG.
Please note that FASTBOOT_USE_BCB_SET_REBOOT_FLAG is mutually exclusive
with some platforms which already have their own implementation of this
function.
Signed-off-by: Roman Kovalivskyi <roman.kovalivskyi@globallogic.com>
|
|
Android 10 adds support for dynamic partitions and in order to support
this userspace fastboot must be used[1]. New tool fastbootd is
included into recovery.
Userspace fastboot works from recovery and is launched if:
1) - Dynamic partitioning is enabled
2) - Boot control block has 'boot-fastboot' value into command field
The bootloader is expected to load and boot into the recovery image
upon seeing boot-fastboot in the BCB command. Recovery then parses the
BCB message and switches to fastbootd mode[2].
Please note that boot script is expected to handle 'boot-fastboot'
command in BCB and load into recovery mode.
Bootloader must support 'reboot fastboot' command which should reboot
device into userspace fastboot to accomodate those changes[3].
Another command that bootloader must support[3] is 'reboot recovery'. This
command should simply reboot device into recovery mode.
[1] - https://source.android.com/devices/bootloader/fastbootd
[2] - https://source.android.com/devices/bootloader/fastbootd#unified_fastboot_and_recovery
[3] - https://source.android.com/devices/bootloader/fastbootd#modifications_to_the_bootloader
Signed-off-by: Roman Kovalivskyi <roman.kovalivskyi@globallogic.com>
Signed-off-by: Roman Stratiienko <r.stratiienko@gmail.com>
Change-Id: I9d2bdc9a6f6f31ea98572fe155e1cc8341e9af76
|
|
Extend fastboot_set_reboot_flag arguments with reboot reason so that
it could handle different reboot cases in future.
Signed-off-by: Roman Kovalivskyi <roman.kovalivskyi@globallogic.com>
|
|
The environment variable loadaddr is in the virtual address space of the
sandbox. To get the actual memory address where the FIT image has been
loaded we have to convert this address according to the memory mapping of
the sandbox.
Equally the addresses in the *.its file have to be converted when used in
the dfu_ram driver.
Signed-off-by: Heinrich Schuchardt <xypron.glpk@gmx.de>
|
|
Function mtdparts_init() is needed for the DFU MTD driver.
Signed-off-by: Heinrich Schuchardt <xypron.glpk@gmx.de>
|
|
Add support for defining raw fastboot partitions in eMMC by specifying
the offset and size in an environment variable. Optionally, the eMMC
hardware partition number may also be specified.
This makes it possible to e.g. update only part of the eMMC boot
partition, instead of having to write the entire partition.
Signed-off-by: Filip Brozovic <fbrozovic@gmail.com>
|
|
When unregister gadget driver in ci_udc, the usb device is not
removed or stop. This causes next "usb start" fails to work.
Add a new interface "usb_remove_ehci_gadget" in usb-uclass to
remove the usb device for DM driver. Using "usb_lowlevel_stop" for
non-DM driver.
Signed-off-by: Ye Li <ye.li@nxp.com>
Signed-off-by: Peng Fan <peng.fan@nxp.com>
|
|
The usb mass storage (f_mass_storage.c) uses fixed usb index 0,
this causes problem while CDNS3 USB controller index is 1.
Modify the API of fsg to pass the controller index.
Reviewed-by: Jun Li <jun.li@nxp.com>
Signed-off-by: Ye Li <ye.li@nxp.com>
Signed-off-by: Peng Fan <peng.fan@nxp.com>
|
|
This is used to support RTL8153B and RTL8154B.
Signed-off-by: Hayes Wang <hayeswang@realtek.com>
|
|
The original rtl_clear_bp() is used to clear the firmware of both
PLA and USB MCU. The new one could clear the firmware of PLA or
USB independently. It is unnecessary to clear firmware, if there
is no one to be updated.
Besides, clear the firmware by writing the relative registers in
bulk.
Signed-off-by: Hayes Wang <hayeswang@realtek.com>
|
|
Some settings of PHY have to work after resetting PHY.
Signed-off-by: Hayes Wang <hayeswang@realtek.com>
|
|
Reset bmu after disabling Tx/Rx. This is used to clear the FIFO of
Tx/Rx. The remained data may be transferred after Tx/Rx is re-enabled.
And it results in garbage data.
Signed-off-by: Hayes Wang <hayeswang@realtek.com>
|
|
If the SCIF is receiving data quickly enough, it may happen that the
SCxSR_RDxF flag is cleared in sh_serial_getc_generic(), while the
FIFO still contains data. If that happens, the serial_getc_check()
reports no data in the FIFO as the flag is no longer set. Add one
more check, if the SCxSR_RDxF is not set, read out the FIFO level
and if there are still characters in the FIFO, permit reading them
out.
Signed-off-by: Marek Vasut <marek.vasut+renesas@gmail.com>
Cc: Nobuhiro Iwamatsu <iwamatsu@nigauri.org>
|
|
Fix this typo in the Kconfig help.
Suggested-by: Wolfgang Wallner <wolfgang.wallner@br-automation.com>
Signed-off-by: Simon Glass <sjg@chromium.org>
Reviewed-by: Bin Meng <bmeng.cn@gmail.com>
|
|
https://gitlab.denx.de/u-boot/custodians/u-boot-ti
- Update to ABI 3.0
- Fix i2c write in eeprom driver
|
|
For proper initialization of aardvark pci driver it is required to
de-assert reset GPIO. So depeneds on DM_GPIO option.
Signed-off-by: Pali Rohár <pali@kernel.org>
Reviewed-by: Stefan Roese <sr@denx.de>
Tested-by: Andre Heider <a.heider@gmail.com>
|
|
- The SDIO signal voltage and max base clock frequency
setting are missing in driver, which causes SDIO
not working.
- The patch adds SDIO signal voltage switch support,
which is based on regulator-gpio of vqmmc-supply, and
sets the max base clock frequency.
- Fix the zero clock value in call to sdhci_setup_cfg()
function.
Change-Id: I79c8860c65b8db166f4f70db56ede4097f71f1fa
Signed-off-by: Evan Wang <xswang@marvell.com>
Reviewed-on: http://vgitil04.il.marvell.com:8080/53589
Reviewed-by: Hua Jing <jinghua@marvell.com>
Tested-by: Hua Jing <jinghua@marvell.com>
[pali: Amended fixup patch]
Signed-off-by: Pali Rohár <pali@kernel.org>
Reviewed-by: Konstantin Porotchkin <kostap@marvell.com>
Reviewed-by: Stefan Roese <sr@denx.de>
Tested-by: Andre Heider <a.heider@gmail.com>
|
|
This change ensures that PCIe card is put into reset state when U-Boot
stops using it.
DM_FLAG_OS_PREPARE ensures that U-Boot executes driver's remove callback
prior booting Linux kernel.
Linux kernel pci-aardvark driver needs to reset PCIe card via PERST# signal
prior initializing it. If it does not issue reset then some PCIe cards
(specially Compex WiFi cards) are not detected at all.
Putting PCIe card into reset state prior booting Linux kernel would ensure
that card would be properly reset at time when Linux kernel starts
initializing pci-aardvark driver.
Signed-off-by: Pali Rohár <pali@kernel.org>
Reviewed-by: Konstantin Porotchkin <kostap@marvell.com>
Tested-by: Andre Heider <a.heider@gmail.com>
|
|
Change active-high to active-low and change DT property name from
reset-gpio to reset-gpios. This format of gpio reset is used by
pci-aardvark driver in Linux kernel.
Signed-off-by: Pali Rohár <pali@kernel.org>
Reviewed-by: Stefan Roese <sr@denx.de>
Reviewed-by: Konstantin Porotchkin <kostap@marvell.com>
Tested-by: Andre Heider <a.heider@gmail.com>
|
|
struct ti_sci_rm_type_map is no longer used. Drop its definition and its
declarations.
Signed-off-by: Lokesh Vutla <lokeshvutla@ti.com>
|
|
With ABI 3.0, sysfw deprecated special resource types used for AM65x
SoC. Instead started using device id as resource type similar to the
convention used in J721E SOC.
Signed-off-by: Lokesh Vutla <lokeshvutla@ti.com>
|
|
There is missing dependency for PCIE_ROCKCHIP which selects
PHY_ROCKCHIP_PCIE which directly depends on ARCH_ROCKCHIP.
WARNING: unmet direct dependencies detected for PHY_ROCKCHIP_PCIE
Depends on [n]: ARCH_ROCKCHIP [=n]
Selected by [y]:
- PCIE_ROCKCHIP [=y] && PCI [=y]
Signed-off-by: Michal Simek <michal.simek@xilinx.com>
Reviewed-by: Tom Rini <trini@konsulko.com>
|