diff options
author | Arun Bharadwaj <arun@gumstix.com> | 2015-04-28 16:55:30 -0700 |
---|---|---|
committer | Tom Rini <trini@konsulko.com> | 2015-05-10 09:58:44 -0400 |
commit | 2a3c25d24240d5e3ee660f0875e755a457b5117e (patch) | |
tree | 6f8d3a092704b46610ab31b5a3461beeab8ba907 /board | |
parent | fe5d488fbef192188bcddb8774154bd5527e468b (diff) |
overo: Fix regression introduced in a6b541b
U-Boot has been broken on Overo boards since commit
a6b541b09022acb6f7c2754100ae26bd44eed1d9.
This is because the gd pointer is not set early enough anymore,
such that the i2c_set_bus_num in get_board_revision can safely
execute. This results in a console hang at SPL and the boot does
not proceed.
This piece of code is anyway necessary only for really old Overo
boards with revision numbers <= 2410 and not required for the newer
boards. For these older boards, u-boot v2014.10 still works fine.
Signed-off-by: Arun Bharadwaj <arun@gumstix.com>
Diffstat (limited to 'board')
-rw-r--r-- | board/overo/common.c | 14 |
1 files changed, 0 insertions, 14 deletions
diff --git a/board/overo/common.c b/board/overo/common.c index bdfa5caf50..f6f6792d09 100644 --- a/board/overo/common.c +++ b/board/overo/common.c @@ -310,20 +310,6 @@ int get_board_revision(void) { int revision; -#ifdef CONFIG_SYS_I2C_OMAP34XX - unsigned char data; - - /* board revisions <= R2410 connect 4030 irq_1 to gpio112 */ - /* these boards should return a revision number of 0 */ - /* the code below forces a 4030 RTC irq to ensure that gpio112 is low */ - i2c_set_bus_num(TWL4030_I2C_BUS); - data = 0x01; - i2c_write(0x4B, 0x29, 1, &data, 1); - data = 0x0c; - i2c_write(0x4B, 0x2b, 1, &data, 1); - i2c_read(0x4B, 0x2a, 1, &data, 1); -#endif - if (!gpio_request(112, "") && !gpio_request(113, "") && !gpio_request(115, "")) { |